The on-line 'Live Power' feed is back up again. However it is reading exactly double what the true output is: the problem was too weak a signal and my workaround has been to put two current transducers in series on the wire from the inverter.
Better to have a reading than no reading !
...experience gained from the operation of a microhydro plant, probably of interest mostly to other Powerspout owners. At the start, in 2014, it was new and there was much to write about but as time has passed there is less. So new posts will only be written if something interesting comes along, - look below to see if there is a new post.
Wednesday, 22 July 2015
Sunday, 19 July 2015
Monitoring problems
Generating at flows lower than I have been able to generate at previously is creating problems with my monitoring systems. For the moment, I haven't been able to quite understand why this should be, but a result of it is that I have removed the feed to the "Live Power" tab on this blog because it was giving wrong readings.
Having an interest in closely following the output of my installation, I monitor output in different ways. Some are convenient but not very accurate whilst others are inconvenient but more accurate.
The convenient, 'at-a-glance' system relies on a Wattson monitor with its feed going also, via a Wattson Anywhere hub, to the web. It is this system which is playing up: when the turbine is happily putting out 160 W, the monitor and web portal sometimes show zero. As can be seen from the online trace below, it suddenly dropped to zero at 17.00 hours on Thursday even though the turbine was in fact OK:
As a backup to Wattson, I also monitor using the blue tooth output from the Sunny Boy inverter : SMA's Sunny Beam system. This is not quite so much 'at-a-glance' and it is not quite as accurate, but it does have the benefit of being able to store several months of data. The Wattson display can also store data but only about three weeks worth. If you don't remember to download the data to your pc within that time, it starts overwriting and readings are lost.
The final system I use, which is the most accurate, is the kWh generation meter used for submitting readings for Feed in Tariff claims. One can use this as a way of measuring power output by noting the exact moment in time when its decimal place updates and then doing a calculation based on the increment in kWh and the precise time interval to achieve this increment (measured in seconds). I usually do readings over at least a 24 hour period and, of course, to be valid, there should have been no change in the turbine's output during this period. Since multiple 24 hour readings give values for power which are within 0.5 W of each other, I think the method is accurate enough.
Unfortunately, this meter too is proving inaccurate at low flows - something which Elster, the manufacturer, makes clear will happen when the current flowing is below 0.5 A.
None of this matters very much except that it's introducing error into my on-going study of 'whole system' efficiency at low flow. In truth, there are probably so many other inaccuracies, especially knowing precisely what the flow is, that this added error will probably not matter very much.
Having an interest in closely following the output of my installation, I monitor output in different ways. Some are convenient but not very accurate whilst others are inconvenient but more accurate.
The convenient, 'at-a-glance' system relies on a Wattson monitor with its feed going also, via a Wattson Anywhere hub, to the web. It is this system which is playing up: when the turbine is happily putting out 160 W, the monitor and web portal sometimes show zero. As can be seen from the online trace below, it suddenly dropped to zero at 17.00 hours on Thursday even though the turbine was in fact OK:
As a backup to Wattson, I also monitor using the blue tooth output from the Sunny Boy inverter : SMA's Sunny Beam system. This is not quite so much 'at-a-glance' and it is not quite as accurate, but it does have the benefit of being able to store several months of data. The Wattson display can also store data but only about three weeks worth. If you don't remember to download the data to your pc within that time, it starts overwriting and readings are lost.
The final system I use, which is the most accurate, is the kWh generation meter used for submitting readings for Feed in Tariff claims. One can use this as a way of measuring power output by noting the exact moment in time when its decimal place updates and then doing a calculation based on the increment in kWh and the precise time interval to achieve this increment (measured in seconds). I usually do readings over at least a 24 hour period and, of course, to be valid, there should have been no change in the turbine's output during this period. Since multiple 24 hour readings give values for power which are within 0.5 W of each other, I think the method is accurate enough.
Unfortunately, this meter too is proving inaccurate at low flows - something which Elster, the manufacturer, makes clear will happen when the current flowing is below 0.5 A.
None of this matters very much except that it's introducing error into my on-going study of 'whole system' efficiency at low flow. In truth, there are probably so many other inaccuracies, especially knowing precisely what the flow is, that this added error will probably not matter very much.
Saturday, 4 July 2015
Post mortem on ceramic bearings
You can learn a lot from a careful inspection of a failed bearing. Yesterday I learned the story of why the trial of ceramic bearings came to an end after just 28 days: - one ball in the bearing at the Smart Drive end of the shaft appeared to have a manufacturing defect:
As the bearing rotated, this defective ball intermittently caused the inner race to 'lock up'. When this happened, the inner race started to turn on its journal on the shaft. Being harder than the stainless steel of the shaft, the journal got ground down:
I had noticed there was a slight 'catch' to smooth rotation of the shaft even before I had installed the housing with the new bearings, so there is reasonable certainty that this defective ball was indeed present from the outset, and did not become damaged during the 28 days of operation.
It's satisfying to have reached an explanation for this premature failure. Just possibly, if it was a manufacturing defect, it might not mean it's totally the end of the road for using ceramics in a Powerspout.
For the moment however, the turbine continues to generate at lower flows than were possible in its first year of operation: presently putting out 223W on 0.96 litres per sec. Nice to see the benefits being realised of the changes made to extend generation into these drier months.
The question now is: how low a flow can I usefully go to ? All will be revealed as the dryness of summer progresses.
As the bearing rotated, this defective ball intermittently caused the inner race to 'lock up'. When this happened, the inner race started to turn on its journal on the shaft. Being harder than the stainless steel of the shaft, the journal got ground down:
I had noticed there was a slight 'catch' to smooth rotation of the shaft even before I had installed the housing with the new bearings, so there is reasonable certainty that this defective ball was indeed present from the outset, and did not become damaged during the 28 days of operation.
It's satisfying to have reached an explanation for this premature failure. Just possibly, if it was a manufacturing defect, it might not mean it's totally the end of the road for using ceramics in a Powerspout.
For the moment however, the turbine continues to generate at lower flows than were possible in its first year of operation: presently putting out 223W on 0.96 litres per sec. Nice to see the benefits being realised of the changes made to extend generation into these drier months.
The question now is: how low a flow can I usefully go to ? All will be revealed as the dryness of summer progresses.
Subscribe to:
Posts (Atom)